A Tale of Two Terriers by Tim Stanger
Mechanical
Division Manager, Tim Stanger, describes the restoration of
our two most historic locomotives, which returned to service
in 1984 after several years of inactivity
First published in issue 35 of The Tenterden Terrier Winter
1984
Reproduced with permission of present editor Mr P D Shaw.
In
common with many members, I believe the Kent and East Sussex
Railway is unthinkable without the sight and sound of a working
Terrier. That may be romantic nonsense, or nostalgia, and certainly
the harsh economic realities of today dictate that more modern
and larger locomotives must be in service to haul trains beyond
the capacity of the Terriers. The locomotive department needs
to produce a balanced fleet to meet the needs of the railway
operation and give visitors an interesting variety of motive
power.
Neither
No.10 “Sutton” nor No.3 “Bodiam” had
seen service in the 1980s, until this year. No.10 had been withdrawn
from service on 01 January 1980 and No.3 some two years earlier
in September 1977 – both requiring a thorough overhaul,
including boiler repairs.
Locomotive
restoration requires three main ingredients; money (and plenty
of it), skilled labour (with a good deal of unskilled labour)
and sheer determination.
As
far as No.10 was concerned, the decision was made by the Board
that the proceeds from the Steam and Country Fair (remember
those?) of September 1981 would be utilised for its restoration.
Although the whether was somewhat unkind, the attraction of
the replica “Rocket” drew the crowds and enabled
the boiler work required to be put out to tender.
By
the end of 1981, “Sutton” had been stripped down
sufficiently for the whole of the boiler and firebox to be thoroughly
examined for six contractors to tender for the work envisaged.
Incidentally, we have found that the dismantling of both Terriers
was no easy task. William Stroudley certainly did not build
them with that in mind – but I digress.
Resco
(Railways) Ltd. won the contract, and the boiler with fittings
was delivered to their Erith works on 01 June 1982, returning
to us in sound order on 04 November 1983. Work at Resco’s,
under the direction of their then boilersmith Norman Payne,
progressed steadily, with a new smokebox being fabricated and
removal of the inner copper firebox with a view to a replacement
steel firebox being made. In the event, on the advice of Resco’s,
the decision was made in January 1983, in conjunction with our
Boiler Inspector, to repair and refit the copper box, together
with 258 replacement copper stays. While this undoubtedly saved
some £1600, it did take time and served to a degree to
delay the return of the boiler.
At
each stage of the boiler/firebox repair, our Boiler Inspector,
Bill Vincent, inspected the work done. New longitudinal stays
and four new palm stays were required as a result of these inspections,
which unfortunately swallowed up much of the savings made, but
as so often is the case, the deeper you dig, the more you find.
Whilst
the frames and motion had been steam cleaned and overhauled,
it was only on the return of the boiler and it reunification
with the frames that restoration could really get under way.
On the face of it, this was a “just” job –
it just needed re-assembling, plumbing up and painting. I dread
to think how many hundreds of hours those “just”
jobs took!
From
the outset of my involvement in the management of Rolvenden
in November 1982, I firmly believed that a project system, with
a Leader for each project, would encourage volunteer involvement
and build small teams that work well together. Bob Forsythe,
as Leader with Lawrence Donaldson and David Brailsford as two
very hard-working right-hand men, pulled in many skilled and
unskilled volunteers to see this project finished.
We
all have an aversion to deadlines, even though they concentrate
the mind wonderfully. The return of “Sutton” to
steam was set for 28 May 1984. The job was finished on time,
in fact, three days early, and on the due day she entered traffic,
with the BBC in attendance in appalling weather.
It
was in July 1982 that John Liddell and I had a meeting with
Ron and Vic Wheele, the owners of No.3 “Bodiam”,
to discuss the restoration of their locomotive. Following a
boiler inspection by Norman Payne, the Board made funds available
for the work to be instigated. In January 1983, Paul Hatcher
was made project leader and dismantling began. By May, the motion
had been overhauled, cab floor platework replaced and the boiler
fittings re-packed and stored. Meanwhile in February, the boiler
had been transported to Resco’s where it was shotblasted
by contractors and painted by volunteers.
The
locomotive had failed in September 1977 due to wastage and leakage
from the boiler front tubeplate flange. Paul Hatcher and Adrian
Landi carried out some repairs at Resco’s for one week,
breaking the back of the work, and a new smokebox was rolled
up at the same time.
While
the tubes appeared good for another two years or so (unlike
No.10’s which had to be scrapped) , platework on the lower
portion of the outer firebox just above the foundation ring
had to be cut out and certified plate let in and welded up.
This was also carried out by Paul and Adrian when the boiler
returned to Rolvenden in November, on the same low-loader as
No.10’s.
Bearing
in mind the considerable winter work involved in the open, it
is a very great achievement that the boiler was finished in
time for its steam test to take place on 25 May 1984 having
passed its hydraulic test some weeks before.
As
with No.10, once the boiler had been completed it “just”
had to be re-assembled, and again many man-hours were worked
to “just put it together”